Case Study: Preventing Damaging Harmonics Note: This Case Study can also be found in the sidebar of the Power Quality Application |
When one of our customers was experiencing high neutral currents, BEST was called out to check and record temperatures on a 150kVA zig zag type transformer. A power quality analyzer was used to determine harmonic amplitudes and waveform distortions. The transformer temperature was 249.5F with a 3rd harmonic RMS 401.6 amps. and a 9th harmonic RMS 124.0 amps.
It was recommended that a 3rd harmonic filter/blocker be installed to reduce the RMS neutral current at the power source, thus reducing the entire systems harmonic load.
After the harmonic blocker was installed the transformer was retested 6 days later. Temperature were reduced by 15.0 degrees F, but most importantly the 3rd harmonic was reduced by 393.6 Amps RMS current to a total of 8 Amps RMS current. With the same loads we saw a reduction in the phase current by 7 to 12% with an increase in power factor and improved current waveform.
The installation will allow the customer to add additional loads without up sizing the electrical system and should see a return on investment in less than 24 months with an increase in transformer life.
Annual savings due to reduction of harmonic current losses:
$ 8,278Annual savings due to reduce need for heat removal:
$ 2,030Total Annual Savings:
$10,308